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Events of 2004

February until May 2004..... Not a very good start to our year I afraid, with a suspect head Gasket, Tyres and a MOT to over come. We had many problems with the Head Gasket repair, in fact it turned into a engine rebuild, which caused us loads of spares availability problems. For those interested I have added a page which covers the up hill battle we had as the repairs commenced  [ Suspect Head Gasket...if only].


May 2004.....The Abertillery District Museum were kind enough to set up a Jones Exhibit through-out the month of May. The displayed consisted of Jones photos past, route maps, uniforms, a ticket machine and lots more historical items. Also we included some of our photos, certificates from our Rallies and a Diary with the names of people we have had the pleasure of meeting every where we have taken our Bus. [ The Abertillery District Museum Jones Exhibit ]


 

June 12th .....We travelled up to Abertillery on the Saturday and attended the Barry Island Transport Rally on the Sunday. On Monday 14th, we parked the bus in Church street Abertillery from 9.00am until 11.00am. The Trophy on the right we won for "Bus travelling the furthest distance to attend"


July 4th .....The "Bluebell Railway" Rally. Our first local rally since getting our bus back from the garage. [ Photo... ]


July 18th ..... We were approached by our Local "Eastbourne Lions Club" several weeks ago to do a "Free Park & Ride" for the Chinese Boat Racing Day. So we took it on [ Read more...]

 


July 25th .....The photo below is the Sunday, we attended the  “Worthing Bus Rally” .

After our visit to the Garage that replaced our Head Gasket, things have gone from bad to worse. Our first “run out” after the “repair” was to Barry Island” in June. That was a total disaster, in so much that we used 175 litres of water to do the journey, and lost the radiator cap as well. Following a trip back to the Garage on returning to Eastbourne, we were fobbed off with the excuse that there was an air lock or  the engine must have a big crack in it to cause the problem. Also, it would be “uneconomical to repair” should they look into it any deeper.

Sadly, we took the Bus away, and thought that this was the end. We missed the next Rally, which was at North Weald. That was a very big Show in Essex, ( mainly London Transport Buses ). We managed to get to the “Bluebell Railway Bus Rally” which was only 20 miles away, but the Bus boiled up after about 5 miles, so that took the shine off things.

August 8th  we struggled to get to the “Lavender Iine” Bus Rally, which, once again was very close, but the Bus still boiled up very quickly. The next Show was at the “New Forest”. We missed this one as it was 110 miles each way.  This was the first time in 4 years that we had failed to attend. August Bank Holiday was busy. We did a local “Festival of Transport” Show at Hellingly which was only 10 miles away, but still the Bus boiled up.

The Monday, we “went for broke”. We took the Bus to Gosport, in Hampshire, just over a hundred miles each way. If it seized up now, that would be it. The Bus had, had a good life, so we went for it. As it was, we had plenty of water on board and it started off a very cold day.  We made plenty of stops for water, and eventually made it.


September,4th, we did our first Wedding, that was a very short driving day, thankfully. It still boiled up !  On Sunday, 12th September, we decided that we would do the “Amberley Bus Rally” and then call it a day. We had done a few Rallies and it was time to give up and look for a replacement engine, somehow.

After that last run, we were approached by an enthusiastic engineer, again, to look at our Bus. He did offer to look at it earlier in the year, but the Bus broke down originally at the Bus Garage that did the work, while we were there, having an estimate being done for a replacement Speedo job. So the Bus stayed there, unable to return.

 The engineer, called John, said that he would look at our Bus “between jobs” and if it was repairable, he would attempt it, but don’t expect miracles over night. I managed to get another Head Gasket, and other bits and bobs, and left it to him.

September 24th, the bus was fired up and was a great delight to listen to. It was so quiet, no water was being pumped out under pressure through the radiator cap, no water being squirted into the Bus interior, no overheating after 20 minutes, BINGO !   At last we had a proper Bus.  This must have been the first time in many years it had run properly.

We  could have done “Duxford Showbus” that weekend, but decided not to chance it without giving it a good running in period first. This was our first time in 5 years that we had missed “Duxford”,  but  it was worth it.

Photo of myself standing next to the Mayor of Worthing, and his Wife.  

The Bus is now up and running in a truly magnificent way and hope that this is now a new beginning for us. We are now trying to catch up on our “Winter maintenance” so that next years’ season will be more successful.  In the meantime, thanks to everyone who have been sending us e-mails in support of our bus. We hope to bring the Bus back to Abertillery in June to do the Barry Island Rally again.
Looking from the Queen's Hotel BlainaAberbeeg

 

We visited a few friends in the area just before Christmas, so we decided to finish off this years events, with a few weather related photos. Happy New  Year... Roger & Sue.

Roger.... Put that away